Helicopter engine failure leads to steep descent and ground impact

Casualties unknown • Mohawk, TN, US

A helicopter experienced a sudden engine failure during the downwind leg of the traffic pattern, resulting in a steep descent and ground impact near a private airstrip.

What happened

After landing at a private airstrip, the flight instructor exited the helicopter while the student pilot remained in the aircraft with the engine running. The instructor then reboarded the aircraft, after which the student performed a takeoff.

While flying on the downwind leg of the traffic pattern, a witness observed a loud noise emanating from the engine. Following this noise, the main rotor was seen to slow significantly, and the helicopter entered a very steep descent. The aircraft impacted the ground approximately 1,000 feet south of the runway. There were no fatalities reported.

The investigation

Investigators examined the engine and found that the rod bolts on the number four cylinder had fractured. A metallurgical examination of one of the rod bolts revealed cracking through 25 percent of the bolt.

An examination of the flight controls showed no evidence of failure prior to the impact. At the time of the accident, the engine had recorded 813 hours since its last major overhaul and 36 hours since its annual inspection.

Findings

  • The fracture of the engine rod bolts was caused by fatigue.
  • The fatigue was attributed to insufficient preload on the bolt.

Probable cause

The engine failure was caused by fatigue cracking in the number four cylinder rod bolts due to insufficient preload.

Frequently asked questions

What happened in the 1988-11-14 Hughes 269C accident near Mohawk, TN?

A helicopter experienced a sudden engine failure during the downwind leg of the traffic pattern, resulting in a steep descent and ground impact near a private airstrip.

What aircraft was involved and where did it happen?

The accident on 1988-11-14 involved a Hughes 269C, registration N9575F, at Mohawk, TN.

What was the probable cause of the accident?

The engine failure was caused by fatigue cracking in the number four cylinder rod bolts due to insufficient preload.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20001213X27186. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

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