Emergency Landing in Peach Orchard Following Engine Failure

Casualties unknown • FT Mill, SC, US

An aircraft engine lost power during an ILS approach, forcing the pilot to perform an emergency landing in a peach orchard, resulting in aircraft damage.

What happened

Two days prior to the accident, the pilot fueled the aircraft type to capacity and completed a short flight to a private airstrip near his residence. Following that flight, the pilot observed fuel on the upper surfaces of both wings, located behind the fuel filler caps. The pilot was aware that fuel had leaked from the thermos-type fuel caps.

During the subsequent flight, while performing an ILS approach to the destination airport, the engine lost power due to fuel exhaustion. The pilot descended below the cloud layer and executed an emergency landing in a peach orchard. The aircraft sustained damage during the impact.

The investigation

The investigation determined that the aircraft had flown 3.63 hours since its last refueling. Although the pilot reported having at least 4.3 hours of fuel on board after the previous refueling, he believed that approximately 5 to 6 gallons of fuel had siphoned from each tank.

Records indicated that Airworthiness Directive 68-13-03 required inspections of the fuel caps for dryness and hardness after every 100 hours of flight. The last recorded entry for compliance with this AD was in 1985 at approximately 2,590 hours. At the time of the accident, the total airframe time was 2,981 hours.

Probable cause

The engine lost power due to fuel exhaustion caused by fuel siphoning from the tanks through leaking thermos-type fuel caps.

Frequently asked questions

What happened in the 1988-11-23 Piper PA-24-250 accident near FT Mill, SC?

An aircraft engine lost power during an ILS approach, forcing the pilot to perform an emergency landing in a peach orchard, resulting in aircraft damage.

What aircraft was involved and where did it happen?

The accident on 1988-11-23 involved a Piper PA-24-250, registration N6711P, at FT Mill, SC.

What was the probable cause of the accident?

The engine lost power due to fuel exhaustion caused by fuel siphoning from the tanks through leaking thermos-type fuel caps.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20001213X27206. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

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