Main Gear Component Failure During Landing Roll

Casualties unknown • Louisville, KY, US

A flight crew experienced significant vibrations during landing after a torque link apex bolt vibrated out of the left main gear assembly.

What happened

Following the completion of landing, the flight crew observed a vibration occurring during the landing roll. Upon inspection, it was discovered that the left main gear torque link apex bolt had vibrated out of the torque link. This mechanical failure allowed the main gear truck to rotate 360 degrees while the aircraft was on the ground.

The investigation

An examination of the components revealed that the nut had stripped off the bolt. Laboratory testing of the hardware showed that the torque link attaching pins contained excessive play. When investigators measured both new and old apex bolts, they determined that the bolts failed to pass the most stringent quality control checks regarding correct thread size.

Findings

Investigators concluded that the loose torque links created excessive vibration, which caused the nut to strip off the bolt. Furthermore, because the threads on the undersized apex bolt were incorrect, the nut was able to shear away the bolt pin that was specifically designed to retain it.

Probable cause

The nut stripped from the bolt due to excessive vibration caused by loose torque links, a condition exacerbated by undersized apex bolt threads that allowed the retaining pin to be sheared away.

Frequently asked questions

What happened in the 1990-01-31 Douglas DC-9-31 accident near Louisville, KY?

A flight crew experienced significant vibrations during landing after a torque link apex bolt vibrated out of the left main gear assembly.

What aircraft was involved and where did it happen?

The accident on 1990-01-31 involved a Douglas DC-9-31, registration N8978E, operated by Eastern Air Lines, Inc, at Louisville, KY.

What was the probable cause of the accident?

The nut stripped from the bolt due to excessive vibration caused by loose torque links, a condition exacerbated by undersized apex bolt threads that allowed the retaining pin to be sheared away.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20001212X22363. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

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