Forced landing and post-crash fire following engine power loss

Casualties unknown • Longmont, CO, US

An aircraft experienced a significant loss of engine power during its initial climb, resulting in a forced landing in a pasture and a subsequent aircraft fire.

What happened

During the initial climb phase following takeoff, the airplane failed to accelerate or climb, operating at a gross weight approximately 50 pounds above the maximum allowable limit. After the pilot executed a crosswind turn at 250 feet AGL, roughly one-half mile beyond the end of the runway, the engine RPM began to decrease steadily.

Because the pilot was unable to restore the engine RPM, a forced landing was conducted in a nearby pasture. During the landing sequence, the aircraft collided with a fence and a ditch, which caused the plane to nose over. The impact resulted in an aircraft fire.

The investigation

An examination of the engine was performed to determine the cause of the power loss. Investigators discovered that the spark plugs were fouled and the magneto impulse coupling was weak. Additionally, the inspection revealed rust and evidence of detonation within the cylinders and on the piston domes, findings which contributed to the degradation of available power.

Probable cause

The loss of engine power was caused by degraded power availability resulting from fouled spark plugs, a weak magneto impulse coupling, and evidence of detonation and rust within the cylinders.

Frequently asked questions

What happened in the 1991-12-22 Stinson 108-1 accident near Longmont, CO?

An aircraft experienced a significant loss of engine power during its initial climb, resulting in a forced landing in a pasture and a subsequent aircraft fire.

What aircraft was involved and where did it happen?

The accident on 1991-12-22 involved a Stinson 108-1, registration N97962, operated by Donald Badtram/stephen Innes, at Longmont, CO.

What was the probable cause of the accident?

The loss of engine power was caused by degraded power availability resulting from fouled spark plugs, a weak magneto impulse coupling, and evidence of detonation and rust within the cylinders.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20001212X18587. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

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