Hard landing following restricted elevator movement

Casualties unknown • Bemidji, MN, US

A crew experienced restricted up-elevator movement during short final approach, leading to an aborted landing and a subsequent hard landing.

What happened

During the short final phase of flight, the crew of the aircraft noticed that the airplane had restricted up-elevator movement. In response to this control issue, the crew initiated a go-around. To manage the pitch for the subsequent landing attempt, the crew relied on power settings rather than elevator deflection. This resulted in an excessive descent rate and airspeed, which led to a hard landing.

The investigation

A post-incident examination of the aircraft revealed that a loose upper elevator stop bolt had made contact with a stringer, which prevented further movement of the control column. Maintenance records indicated that extensive work had been performed on the elevator quadrant sixteen flights prior to the accident. During that maintenance procedure, hardware was loosely installed on the quadrant to prevent loss. The investigation found that the position of a nut running down on the bolt closely resembled the appearance of a nut that had been properly torqued.

Probable cause

A loose upper elevator stop bolt, which had been improperly secured during previous maintenance work, contacted a stringer and restricted control column movement, leading to an excessive descent rate and airspeed during landing.

Frequently asked questions

What happened in the 1995-12-28 Fairchild SA227-AC accident near Bemidji, MN?

A crew experienced restricted up-elevator movement during short final approach, leading to an aborted landing and a subsequent hard landing.

What aircraft was involved and where did it happen?

The accident on 1995-12-28 involved a Fairchild SA227-AC, registration N159MC, operated by Mesaba Airlines, Inc., at Bemidji, MN.

What was the probable cause of the accident?

A loose upper elevator stop bolt, which had been improperly secured during previous maintenance work, contacted a stringer and restricted control column movement, leading to an excessive descent rate and airspeed during landing.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20001207X04970. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

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