Engine power loss during takeoff following fuel valve installation

Casualties unknown • Anchorage, AK, US

An aircraft experienced engine power loss at 300 feet above the ground after the pilot failed to verify the fuel quantity in the left wing tank prior to departure.

What happened

Following the installation of a new fuel valve, a mechanic placed 10 gallons of fuel in each wing tank to facilitate testing and installation procedures. Before takeoff, the pilot filled the right fuel tank but did not visually verify the amount of fuel remaining in the left tank.

The pilot conducted taxi and runup procedures for approximately 15 minutes with the left fuel tank selected. After completing the takeoff, the engine lost power once the aircraft reached an altitude of 300 feet. Upon the loss of power, the pilot switched to the right fuel tank, which restored some engine power. Due to the low altitude, the pilot focused on performing a forced landing.

The investigation

An examination of the engine revealed no mechanical failures. Investigators determined that the left fuel tank contained 15 gallons of fuel at the time of the incident. It was noted that the left wing tip was resting on the ground and that the fuel tanks interconnect through the fuel valve even when the valve is in the off position.

Findings

The aircraft owner's operating manual includes a pre-takeoff checklist stating that the fuel selector should be set to the tank containing the greatest amount of fuel.

Probable cause

The engine power loss was caused by the pilot's failure to verify the fuel quantity in the left wing tank prior to takeoff, combined with the fact that the left wing tip was resting on the ground.

Frequently asked questions

What happened in the 1996-04-11 Stinson ST-75 accident near Anchorage, AK?

An aircraft experienced engine power loss at 300 feet above the ground after the pilot failed to verify the fuel quantity in the left wing tank prior to departure.

What aircraft was involved and where did it happen?

The accident on 1996-04-11 involved a Stinson ST-75, registration N235C, at Anchorage, AK.

What was the probable cause of the accident?

The engine power loss was caused by the pilot's failure to verify the fuel quantity in the left wing tank prior to takeoff, combined with the fact that the left wing tip was resting on the ground.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20001208X05495. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

Loading the flight search…