Pitch Trim Control System Failure During Descent

Casualties unknown • Dayton, OH, US

A flight crew experienced a loss of pitch trim control while en route, leading to the horizontal stabilizer being locked in its last set position.

What happened

While en route, the flight crew encountered a failure of the pitch trim control system. The crew found themselves unable to adjust the pitch trim using either the switches mounted on the yoke or the horizontal stabilizer control handles located on the center console. This loss of functionality was specifically noted by the crew when they attempted to extend the slats during the descent phase of the flight.

The investigation

An examination of the horizontal stabilizer pitch trim system revealed that there was no lubrication present on the screw actuator assemblies. Investigators determined that a fuse pin had sheared within the output drive unit of the horizontal stabilizer drive gearbox. This shearing of the fuse pin caused the horizontal stabilizer to lock in its final set position, which is the intended design function of the component upon failure.

Further investigation into the manufacturing process involved a review of Assembly Orders at Douglas Aircraft (DAC). The records showed that both DAC production personnel and DAC inspection personnel had stamped the assembly orders to certify that the lubrication process had been completed and accepted. However, the physical evidence confirmed that no lubrication had actually been applied to the screw actuator nuts.

Probable cause

The failure was caused by the lack of lubrication on the screw actuator assemblies, which led to a sheared fuse pin in the horizontal stabilizer drive gearbox output drive unit.

Frequently asked questions

What happened in the 1996-11-08 Mcdonnell Douglas MD-11 accident near Dayton, OH?

A flight crew experienced a loss of pitch trim control while en route, leading to the horizontal stabilizer being locked in its last set position.

What aircraft was involved and where did it happen?

The accident on 1996-11-08 involved a Mcdonnell Douglas MD-11, registration N814DE, at Dayton, OH.

What was the probable cause of the accident?

The failure was caused by the lack of lubrication on the screw actuator assemblies, which led to a sheared fuse pin in the horizontal stabilizer drive gearbox output drive unit.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20001208X07045. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

Loading the flight search…