Left wing drop leads to forced landing in open field

Casualties unknown • Houston, MS, US

A pilot experienced a sudden left wing drop during a forced landing attempt after an aileron control failure caused the aircraft to strike the ground.

What happened

While flying at an altitude of approximately 150 to 200 feet, the pilot performed an aileron input significant enough to cause fluid in the hopper tank to slosh. Following this input, the aircraft began to shudder as if experiencing a stall. The pilot attempted to increase airspeed by moving the control stick forward, but the shuddering persisted and the airplane began a left turn.

In an attempt to correct the flight path, the pilot applied right aileron and rudder. A visual inspection of the ailerons revealed that both were in the up position. Upon reducing power, the left wing dropped. The pilot subsequently increased power and applied rudder to maintain control, but the aircraft continued in a slight left turn. During the execution of a forced landing in an open field, the pilot reduced power once more; at this time, the left wing dropped and collided with the ground. There were no injuries reported.

The investigation

An examination of the aircraft revealed that the left aileron control rod end fitting had become disconnected at the adjustment jam nut. The investigation determined that the rod end had lost its necessary flexibility due to rust and corrosion, resulting from a lack of proper attention or lubrication.

Probable cause

The left aileron control rod end fitting became disconnected at the adjustment jam nut because corrosion caused the rod end to lose its flexibility.

Frequently asked questions

What happened in the 1998-03-04 Cessna 188B accident near Houston, MS?

A pilot experienced a sudden left wing drop during a forced landing attempt after an aileron control failure caused the aircraft to strike the ground.

What aircraft was involved and where did it happen?

The accident on 1998-03-04 involved a Cessna 188B, registration N53382, at Houston, MS.

What was the probable cause of the accident?

The left aileron control rod end fitting became disconnected at the adjustment jam nut because corrosion caused the rod end to lose its flexibility.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20001211X09736. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

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