Engine Power Loss During Spray Calibration Test Leads to Gear Collapse

Casualties unknown • Atlanta, NE, US

An aircraft experienced a substantial loss of engine power at low altitude during a calibration test, resulting in a gear collapse and wing impact upon landing.

What happened

During a sprayer calibration test, the engine of the aircraft suffered a substantial loss of power. At the time of the power loss, the pilot was operating at an altitude of approximately 50 feet above ground level (agl). The pilot reported being at too low an altitude to troubleshoot the power loss or maneuver the aircraft into an open field.

Upon touchdown, the left main gear dug into soft mud. This caused the left main gear to collapse, which subsequently led to the left wing impacting the terrain. The pilot stated that the aircraft rotated approximately 80 degrees about the left wing before coming to a complete stop. The pilot was not injured.

The investigation

Post-accident investigation focused on the engine's performance and the fuel system. Investigators found that the engine would not sustain power at idle or any other power setting when the fuel boost pump was in the 'Off' position.

An examination of the fuel system revealed that a 'B' nut on the fuel line, running from the firewall to the back of the engine, was loose. Following the tightening of this nut, the engine performed correctly at all power settings with the fuel pump in the 'Off' position. No other anomalies were identified in the aircraft or engine.

Probable cause

A loose B-nut on the fuel line caused a loss of engine power during flight.

Frequently asked questions

What happened in the 1998-07-11 Cessna 188B accident near Atlanta, NE?

An aircraft experienced a substantial loss of engine power at low altitude during a calibration test, resulting in a gear collapse and wing impact upon landing.

What aircraft was involved and where did it happen?

The accident on 1998-07-11 involved a Cessna 188B, registration N9247R, at Atlanta, NE.

What was the probable cause of the accident?

A loose B-nut on the fuel line caused a loss of engine power during flight.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20001211X10498. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

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