Engine Failure and Forced Landing in Cotton Field

Casualties unknown • Bruce, MS, US

An engine failure caused by lubrication distress led to a forced landing in a cotton field after the aircraft lost power at low altitude.

What happened

After completing the spraying of a field, the pilot of the aircraft pulled up and deactivated the spray pump. At that moment, the engine experienced a loss of oil pressure accompanied by a loud noise. Smoke began emitting from the cowling, and the engine lost power while the aircraft was approximately 50 feet above the ground.

The pilot performed a forced landing into a cotton field. During the course of the landing roll, the airplane moved through small trees and brush before coming to a final stop across a ditch. The occupants were not injured.

The investigation

An examination of the engine identified that the engine had suffered lubrication distress affecting the number 2 connecting rod bearing and journal. The oil supply for the number 2 connecting rod was provided by the number 2 main bearing. Investigators determined that the number 2 main bearing had shifted within the crankcase bearing saddle, which resulted in a restriction of the oil feed to the number 2 connecting rod. This restriction caused the failure of the number 2 connecting rod.

Probable cause

The engine failure was caused by the number 2 main bearing shifting in its saddle, which restricted oil flow and led to the failure of the number 2 connecting rod bearing.

Frequently asked questions

What happened in the 1999-05-14 Cessna T188C accident near Bruce, MS?

An engine failure caused by lubrication distress led to a forced landing in a cotton field after the aircraft lost power at low altitude.

What aircraft was involved and where did it happen?

The accident on 1999-05-14 involved a Cessna T188C, registration N1994J, operated by Darren L. Collins, at Bruce, MS.

What was the probable cause of the accident?

The engine failure was caused by the number 2 main bearing shifting in its saddle, which restricted oil flow and led to the failure of the number 2 connecting rod bearing.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20001212X18691. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

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