Aircraft Stall and Ground Impact Following Engine Power Loss

Casualties unknown • Elko, NV, US

An aircraft experienced a left wing stall and fell 50 feet to the ground during an attempted return to the runway after failing to produce full power during takeoff.

What happened

The flight was the first operation following the completion of an annual inspection. Prior to the initial takeoff, the pilot performed taxi tests and noted no discrepancies. The engine started easily and operated smoothly at lower RPM settings. An engine run-up, including a magneto check, was completed without any anomalies.

During the takeoff roll, the pilot observed that the engine failed to produce full power, noting that the RPM did not exceed 1,600. The pilot elected to continue the takeoff and subsequently attempted to turn the aircraft back toward the runway to land. While performing a crosswind to downwind turn, the left wing stalled. This resulted in the airplane pitching down and falling approximately 50 feet to the ground. There were no injuries reported.

The investigation

An inspection of the engine revealed weak compression in two cylinders. Further examination identified leaks originating from both the intake and exhaust valves within those two cylinders. No other discrepancies were found during the mechanical examination.

Probable cause

The engine failed to produce full power due to weak compression and valve leaks, leading to a wing stall during an attempted return to the runway.

Frequently asked questions

What happened in the 1999-06-19 Piper J3C-65 accident near Elko, NV?

An aircraft experienced a left wing stall and fell 50 feet to the ground during an attempted return to the runway after failing to produce full power during takeoff.

What aircraft was involved and where did it happen?

The accident on 1999-06-19 involved a Piper J3C-65, registration N26842, operated by Arthur Schwandt, at Elko, NV.

What was the probable cause of the accident?

The engine failed to produce full power due to weak compression and valve leaks, leading to a wing stall during an attempted return to the runway.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20001212X19033. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

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