Floatplane excursion following flap selector error

Casualties unknown • Port Alsworth, AK, US

A pilot attempting a takeoff from a remote lake struck a bank after the aircraft's flaps retracted during the water run.

What happened

The pilot was attempting to perform a takeoff from a remote lake when the hydraulically actuated flaps on the aircraft retracted from the fully extended takeoff position to a 1/2 position at the start of the water run. The pilot reported that the airplane reached the 'on step' phase normally and he subsequently attempted to pump the flaps back to the fully extended position.

However, the aircraft failed to become airborne. During this process, the pilot realized that the flap selector handle was in the 'up' position rather than the required 'down' position. As a result of the failure to lift off, the airplane struck a four-foot-high bank at the end of the lake. The impact caused the floats to separate from the aircraft. The pilot was not injured.

Findings

The investigation focused on the positioning of the flap selector handle. While the pilot initially indicated that he had forgotten to switch the handle to the 'down' position, a later statement suggested that he believed he had positioned it correctly. He noted that his shirt sleeve may have snagged the handle and inadvertently repositioned it during the takeoff run.

Probable cause

The flap selector handle was moved to the up position, likely by the pilot's shirt sleeve snagging the control, which prevented the aircraft from achieving sufficient lift for takeoff.

Frequently asked questions

What happened in the 1999-08-20 DE Havilland DHC-3T accident near Port Alsworth, AK?

A pilot attempting a takeoff from a remote lake struck a bank after the aircraft's flaps retracted during the water run.

What aircraft was involved and where did it happen?

The accident on 1999-08-20 involved a DE Havilland DHC-3T, registration N888KA, operated by Ketchum Air Service, Inc., at Port Alsworth, AK.

What was the probable cause of the accident?

The flap selector handle was moved to the up position, likely by the pilot's shirt sleeve snagging the control, which prevented the aircraft from achieving sufficient lift for takeoff.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20001212X19409. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

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