DC-9 Nose Damage Following Tug Collision During Boarding

Casualties unknown • Minneapolis, MN, US

A DC-9 sustained substantial damage to its nose section after an aircraft tug lurched into the parked aircraft during ground operations.

What happened

During passenger boarding, a DC-9 was parked and being prepared for departure. While a tug driver was maneuvering the vehicle into position to connect the tow bar for pushback, the tug suddenly lurched forward into the parked aircraft. The impact was severe enough that pieces of the aircraft protruded through the tug's windshield, pinning the driver in his seat.

The driver reported being unable to shift the vehicle into reverse and noted that his leg remained pinned against the accelerator pedal. Nearby ground workers attempted to shut off the engine, but the vehicle continued to move forward until the engine was successfully stopped. During the collision, the pilot applied the aircraft brakes upon noticing the unplanned movement. The impact pushed the aircraft backward approximately 30 feet, resulting in substantial damage to the nose section of the fuselage.

The investigation

Following the accident, the tug was placed on jacks for a mechanical inspection. Investigators discovered that the engine shutoff switch failed to stop the engine when it was operated at high throttle settings. Additionally, testing revealed that the braking system was unable to stop the rotation of the drive wheels when the engine was at high throttle.

While these mechanical failures were identified, no anomalies were found during the inspection that could specifically explain the initial lurching described by the driver. Records indicated that this specific tug had been involved in a previous incident involving aircraft damage, where it also reportedly lurched while positioning for a tow bar connection. The manufacturer stated they had no records of operational problems or a known history of lurching issues associated with this model of tug.

Probable cause

The engine shutoff switch failed to stop the engine at high throttle settings and the braking system was unable to stop the drive wheels at high throttle, causing the tug to lurch into the aircraft.

Frequently asked questions

What happened in the 2001-05-01 Douglas DC-9-31 accident near Minneapolis, MN?

A DC-9 sustained substantial damage to its nose section after an aircraft tug lurched into the parked aircraft during ground operations.

What aircraft was involved and where did it happen?

The accident on 2001-05-01 involved a Douglas DC-9-31, registration N9333, at Minneapolis, MN.

What was the probable cause of the accident?

The engine shutoff switch failed to stop the engine at high throttle settings and the braking system was unable to stop the drive wheels at high throttle, causing the tug to lurch into the aircraft.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20010507X00887. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

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