Engine failure and tree impact following propeller overspeed

Casualties unknown • Waco, TX, US

An aircraft experienced an engine/propeller RPM overspeed during a climb, leading to a loss of altitude and an impact with trees near the runway departure end.

What happened

Shortly after departing the runway, the aircraft was climbing at 90 knots when the engine and propeller RPM began to overspeed. The pilot attempted to adjust the propeller control, but the RPM did not change. Consequently, the airplane lost altitude and struck trees located near the departure end of the runway.

The investigation

Post-accident examination of the wreckage identified that the #6 connecting rod had failed. Investigators found no oil present in the engine, and remnants of a gasket were found where the oil filter converter plate should have been.

The engine had undergone factory remanufacture on May 5, 2000, and had logged approximately 376.2 hours since that date at the time of the accident. An investigation into the engine maintenance records showed that an Airworthiness Directive (AD) regarding the oil filter converter plate gasket had not been complied with since the engine's remanufacture.

Findings

The relevant AD addressed the oil filter converter plate gasket on engines factory remanufactured after April 1, 1999. The directive required the replacement of the gasket before further flight on engines exceeding 50 hours since new, overhaul, or the last gasket/converter plate replacement, with subsequent replacements required every 50 hours of service. Failure to comply with this AD could lead to a protruding or swelling gasket, resulting in the loss of engine oil.

Probable cause

The failure to comply with an Airworthiness Directive regarding the replacement of the oil filter converter plate gasket led to engine oil loss and subsequent engine failure.

Frequently asked questions

What happened in the 2001-09-21 Piper PA-32R-301 accident near Waco, TX?

An aircraft experienced an engine/propeller RPM overspeed during a climb, leading to a loss of altitude and an impact with trees near the runway departure end.

What aircraft was involved and where did it happen?

The accident on 2001-09-21 involved a Piper PA-32R-301, registration N192SP, operated by Michael L. Oatman, at Waco, TX.

What was the probable cause of the accident?

The failure to comply with an Airworthiness Directive regarding the replacement of the oil filter converter plate gasket led to engine oil loss and subsequent engine failure.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20010926X01992. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

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