Single Engine Missed Approach Accident Following Right Engine Power Loss

Casualties unknown • Sturgis, MI, US

An aircraft experienced a loss of power in the right engine during the departure climb, leading to an attempted single-engine missed approach under instrument conditions.

What happened

During the departure climb phase of flight, the pilot experienced a loss of power in the right engine. Following this failure, the pilot attempted a single-engine missed approach back to the departure airport. The pilot reported being high on the approach and subsequently feathered the propeller when executing the missed approach. At the time of the accident, instrument meteorological conditions (IMC) were prevailing.

The investigation

An examination of the right engine identified that the oil return line, which runs from the turbocharger to the scavende oil pump, had become disconnected. There was no evidence of stripped threads on the connectors. Upon removal of the engine's oil pan, investigators discovered metallic debris inside. Maintenance records indicated that the last recorded maintenance for this engine was its installation 31.7 hours before the accident.

Findings

Performance data analysis for the aircraft showed that under field conditions and in a single-engine climb configuration, the aircraft had a positive climb rate of approximately 340 fpm. However, the data also demonstrated that if the propeller is not feathered, there is a loss of single-engine climb performance of 400 fpm. Additionally, using a flap setting of 15 degrees results in a further loss of 200 fpm.

Probable cause

The disconnection of the oil return line from the turbocharger to the scavenge oil pump, which led to the loss of power in the right engine.

Frequently asked questions

What happened in the 2002-01-06 Cessna 414A accident near Sturgis, MI?

An aircraft experienced a loss of power in the right engine during the departure climb, leading to an attempted single-engine missed approach under instrument conditions.

What aircraft was involved and where did it happen?

The accident on 2002-01-06 involved a Cessna 414A, registration N6560C, at Sturgis, MI.

What was the probable cause of the accident?

The disconnection of the oil return line from the turbocharger to the scavenge oil pump, which led to the loss of power in the right engine.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20020109X00050. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

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