Engine failure and forced landing of aircraft on I-20 West

Casualties unknown • Morton, MS, US

A pilot performed an emergency forced landing on a highway after experiencing engine power loss and smoke in the cockpit.

What happened

While operating in cruise flight, the pilot reported that the engine began running roughly and losing power. Smoke entered the cockpit, accompanied by a clanking noise originating from the engine. The pilot subsequently elected to perform a forced landing on I-20 West. During the descent, the pilot failed to extend the landing gear, resulting in the aircraft striking the guard railing separating the eastbound and westbound lanes. The impact caused substantial damage to the fuselage and wings.

The investigation

The engine was removed and sent to Textron Lycoming for examination. An inspection of the number one and number four spark plugs revealed oil and heavy carbon debris. Heavy carbon debris was also identified in the exhaust valve guide area. Investigators found that the number four exhaust valve was stuck in the open position. The tip of the number four exhaust valve exhibited damage signatures consistent with operating without the rotator cap; the cap was later located at the bottom of the number four rocker cover.

Upon examination with an optical comparator in the Lycoming Metrology laboratory, the number four exhaust valve stem appeared straight. However, the number four piston dome showed a circular mark consistent with an impact from the exhaust valve. Additionally, the number four cylinder exhaust push rod and shroud tube were found broken and separated from the engine upon receipt. The hydraulic lifter for the number four cylinder exhaust was also found to be below minimum leak down specifications.

Probable cause

The engine failure was caused by a stuck exhaust valve, which resulted in an impact between the valve and the piston dome.

Frequently asked questions

What happened in the 2002-09-11 Piper PA24-250 accident near Morton, MS?

A pilot performed an emergency forced landing on a highway after experiencing engine power loss and smoke in the cockpit.

What aircraft was involved and where did it happen?

The accident on 2002-09-11 involved a Piper PA24-250, registration N5724P, operated by Steve Ray Smith, at Morton, MS.

What was the probable cause of the accident?

The engine failure was caused by a stuck exhaust valve, which resulted in an impact between the valve and the piston dome.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20020912X01594. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

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