In-flight depressurization and nose gear indication during takeoff from Denver

Casualties unknown • Denver, CO, US

A flight departing Denver experienced cabin depressurization and a nose gear warning shortly after takeoff, though the aircraft landed safely.

What happened

Shortly after takeoff, the crew of a Boeing 737 (registration not provided) heard a loud bang, which was immediately followed by a loss of cabin pressurization. During the event, the pilots observed an unsafe nose gear indication on the instrument panel.

In response to the indication, the pilots moved the landing gear handle to the down position and subsequently received three green lights, confirming the gear was locked. To verify the status of the aircraft, the control tower monitored a low pass, which confirmed that the landing gear remained in the down position. The flight eventually completed an uneventful landing at Denver.

The investigation

Post-accident examination conducted by maintenance personnel identified a hole in the forward pressure bulkhead and a broken nose gear actuator. Specifically, investigators found that the piston rod of the nose landing gear actuator had worn threads. Additionally, a key locking washer within the gear assembly was found to have sheared. The airline reported that these components were part of the original equipment.

Probable cause

The failure of a key locking washer in the gear assembly and worn threads on the nose gear actuator piston rod led to a broken actuator and a hole in the forward pressure bulkhead.

Frequently asked questions

What happened in the 2005-05-14 Mcdonnell Douglas MD-88 accident near Denver, CO?

A flight departing Denver experienced cabin depressurization and a nose gear warning shortly after takeoff, though the aircraft landed safely.

What aircraft was involved and where did it happen?

The accident on 2005-05-14 involved a Mcdonnell Douglas MD-88, registration N949DL, at Denver, CO.

What was the probable cause of the accident?

The failure of a key locking washer in the gear assembly and worn threads on the nose gear actuator piston rod led to a broken actuator and a hole in the forward pressure bulkhead.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20050526X00682. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

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