Stinson 108 runway excursion and inversion

Casualties unknown • Meadville, PA, US

A Stinson 108 aircraft departed the runway and overturned during its landing roll following a mechanical failure of the tailwheel assembly.

What happened

During the landing roll, the Stinson 108 began an uncontrolled left turn. The pilot attempted to counter the turn by applying opposite rudder, but the maneuver was unsuccessful. The aircraft subsequently departed the runway and struck a ditch, which caused the airplane to nose over and come to rest in an inverted position.

The investigation

An examination of the wreckage focused on the tailwheel assembly. Investigators found that the tailwheel spring clips had disconnected from the tailwheel springs; these components were noted to be stretched and distorted. The investigation revealed that approximately two weeks prior to the accident, the owner had installed a new tailwheel. During this installation, the owner chose not to use the new spring clips provided in the kit, opting instead to reuse the existing clips from the aircraft. It was determined that the owner was not a certificated mechanic and did not consult a professional mechanic during the installation process.

Findings

Findings indicated that the tailwheel spring clips had failed due to being reused rather than using the new hardware provided with the kit.

Probable cause

The failure of the tailwheel spring clips, which had been improperly reused from a previous installation, caused the tailwheel assembly to malfunction during the landing roll.

Frequently asked questions

What happened in the 2006-08-11 Stinson 108 accident near Meadville, PA?

A Stinson 108 aircraft departed the runway and overturned during its landing roll following a mechanical failure of the tailwheel assembly.

What aircraft was involved and where did it happen?

The accident on 2006-08-11 involved a Stinson 108, registration N97541, at Meadville, PA.

What was the probable cause of the accident?

The failure of the tailwheel spring clips, which had been improperly reused from a previous installation, caused the tailwheel assembly to malfunction during the landing roll.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20060912X01328. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

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