Cargo shift causes minor damage to Boeing 737 bulkhead during descent

Casualties unknown • En route to Edinburgh Airport, GB

A cargo unit shifted forward in a Boeing 737-400 during descent into Edinburgh, striking the forward bulkhead and causing minor damage.

What happened

On 26 April 2024, a Boeing 737-4K5, registration G-JMCZ, was performing a commercial cargo flight from London Stansted to Edinburgh. As the crew initiated the descent into Edinburgh, they heard a loud, double-impact noise accompanied by a momentary increase in vibration on the right engine. While the crew initially considered an engine surge, they also suspected a potential cargo shift within the main deck.

The aircraft landed safely at Edinburgh without any further issues. Upon arrival, during the unloading process, ground personnel discovered that a unit load device (ULD) originally positioned in Bay B had moved into Bay A. This movement caused minor damage to the paint and liner tape on the forward bulkhead.

The investigation

The investigation examined the aircraft' and the loading procedures. The Boeing 737-4K5 had been configured for cargo, featuring a bulkhead between the large cargo door and the forward aircraft door. At the time of the incident, the aircraft was loaded with 8,944 kg of cargo, with Bay A left as a void space.

Investigators found that the aircraft's centre of gravity remained within safe manufacturer limits despite the shift, and no handling difficulties were experienced by the crew. Because the cargo was unloaded before the crew could inspect the locks, it could not be determined if the movement was due to a mechanical failure of the locks or human error during the securing process. The investigation noted that the physical layout of the cargo deck makes it difficult for crew to visually verify the security of all locks once the main deck is loaded.

Findings

  • The ULD in Bay B moved forward into the empty Bay A during the descent phase.
  • The ULD locks in Bay B were likely not properly secured, allowing the unit to slide forward when the aircraft pitched down.
  • The shift resulted in no injuries and only minor damage to the forward bulkhead's interior surface.
  • The operator's procedures for managing void bays were reviewed to mitigate the risk of similar occurrences.

Probable cause

The cargo shift was likely caused by the failure to properly secure the floor locks for the ULD in Bay B, allowing it to move into the adjacent void bay during descent.

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Frequently asked questions

What happened in the 2024-04-26 Boeing 737-4K5 accident near En route to Edinburgh Airport, GB?

A cargo unit shifted forward in a Boeing 737-400 during descent into Edinburgh, striking the forward bulkhead and causing minor damage.

What aircraft was involved and where did it happen?

The accident on 2024-04-26 involved a Boeing 737-4K5, registration G-JMCZ, at En route to Edinburgh Airport, GB.

What was the probable cause of the accident?

The cargo shift was likely caused by the failure to properly secure the floor locks for the ULD in Bay B, allowing it to move into the adjacent void bay during descent.

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