Engine separation and crash during training mission from Loring AFB

4 fatalities • Loring AFB, United States of America • Takeoff (climb)

A training flight departing Loring Air Force Base resulted in a fatal crash after mechanical failure led to the loss of two engines.

What happened

A scheduled six-hour training mission departed Loring AFB at 0900LT. During the initial climb phase, the aircraft encountered intense turbulence. During this period, the drag brace for the number three engine failed because a nut was missing from the assembly. This failure caused the third engine to shift upward in front of the wing, which induced a heavy roll to the left.

In an effort to stabilize the aircraft, the crew applied aggressive control inputs. These maneuvers led to the separation of both the number three and number four engines from the wing. Following this structural failure, the aircraft entered a 90-degree right bank and descended into a forested area located approximately 2.4 miles north of the runway. The impact resulted in the total destruction of the aircraft and four fatalities among the crew.

Findings

The investigation determined that the sequence of events began when the engine drag brace failed due to a missing nut.

Probable cause

The failure of the number three engine drag brace caused by a missing nut led to engine separation and subsequent loss of control.

Frequently asked questions

What happened in the 1965-01-04 Boeing KC-135 Stratotanker accident near Loring AFB, United States of America?

A training flight departing Loring Air Force Base resulted in a fatal crash after mechanical failure led to the loss of two engines.

Were there any fatalities in the 1965-01-04 Boeing KC-135 Stratotanker accident?

The accident was fatal, resulting in 4 fatalities.

What aircraft was involved and where did it happen?

The accident on 1965-01-04 involved a Boeing KC-135 Stratotanker, registration 61-0265, operated by United States Air Force - USAF (since 1947), at Loring AFB, United States of America.

What was the probable cause of the accident?

The failure of the number three engine drag brace caused by a missing nut led to engine separation and subsequent loss of control.

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