Tail rotor driveshaft failure causes helicopter spin at Beverley Airfield

Casualties unknown • Beverley Airfield, East Yorkshire, GB

An Enstrom F-28A helicopter experienced a sudden loss of yaw control shortly after takeoff, resulting in a 360-degree rotation and a heavy landing.

What happened

On 10 May 2008, a private flight departed from Beverley Airfield in East Yorkshire. After completing necessary pre-flight and power checks, the pilot of the Enstrom F-28A, registration G-BRZG, increased power and raised the collective lever to lift off.

As the helicopter ascended a few feet above its takeoff position, the pilot encountered immediate difficulty maintaining directional control, noting a significant yaw to the left. Attempts to correct this movement using the left pedal were unsuccessful. Fearing a malfunction within the tail rotor system, the pilot reduced power and fully lowered the collective lever. This action resulted in the helicopter rotating through a full 360-degree turn before making a heavy landing on its skids. The aircraft remained in a level attitude upon impact, and the pilot, who sustained no injuries, exited the aircraft via the side door.

The investigation

Following the incident, the aircraft's yaw control system underwent a thorough inspection. A metallurgical examination was performed on several components, including the flexible coupling assembly, by a materials specialist.

Investigators found that one of the tail rotor blades was severely bent and showed marks suggesting it had struck a multi-stranded control cable. However, the cause of this contact remained unclear. Further technical analysis revealed that the tail rotor driveshaft had fractured within the hub of the flexible coupling. The examination of the driveshaft and coupling components, including hardness and elemental analysis, showed no evidence of pre-existing defects.

Findings

  • The tail rotor driveshaft failed due to torsional overload.
  • The fracture pattern was consistent with the shaft failing in shear because of excessive torque, likely caused by the tail rotor striking an object.
  • No pre-existing mechanical defects were identified that could have caused the initial yaw control issues.
  • The heavy landing resulted in damage to the skids, the tail rotor, and the tail rotor drive.

Probable cause

The tail rotor driveshaft failed due to excessive torque, which caused the loss of yaw control and the subsequent uncontrolled rotation of the helicopter.

Frequently asked questions

What happened in the 2008-05-10 Enstrom F-28A accident near Beverley Airfield, East Yorkshire, GB?

An Enstrom F-28A helicopter experienced a sudden loss of yaw control shortly after takeoff, resulting in a 360-degree rotation and a heavy landing.

What aircraft was involved and where did it happen?

The accident on 2008-05-10 involved a Enstrom F-28A, registration G-BRZG, at Beverley Airfield, East Yorkshire, GB.

What was the probable cause of the accident?

The tail rotor driveshaft failed due to excessive torque, which caused the loss of yaw control and the subsequent uncontrolled rotation of the helicopter.

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