Pilot ejects from glider during unexpected stall near Bystřice

Casualties unknown • NNW obce Bystřice (okres Benešov), CZ

A pilot was forced to bail out of a DG-400 glider after the aircraft entered an unrecoverable descent during thermal soaring.

What happened

On August 14, 2011, a DG-40 and glider, registration OK-2154, was engaged in a thermal soaring flight near Benešov. After being towed from Benešov Airport (LKBE) and releasing from the tow plane at approximately 600 meters AGL, the pilot began searching for thermal currents in the area south of the airfield.

While flying in a light thermal updraft with flaps set to +6°, the pilot noticed the aircraft began to pitch forward and transitioned into a steep, uncontrolled descent. The change in flight characteristics occurred without warning. As the aircraft's descent rate increased, the pilot attempted to recover by repeatedly pulling back on the control stick. However, the descent rate continued to accelerate.

At an altitude of approximately 400 meters AGL and a speed of 150–160 km/h, the pilot jettisoned the cockpit canopy and exited the aircraft. The glider struck an unharvested cornfield approximately 250 meters from residential buildings, landing on its back at an angle of 10–15°. The pilot successfully deployed a parachute and landed approximately 500 meters from the aircraft's impact site. There were no injuries to the pilot.

The investigation

The ÚZPLN investigation relied on pilot testimonies, wreckage examination, and a technical inspection of the aircraft. The investigation included a review of the DG-400 flight manual and consultations with pilots experienced in this specific glider type. Technical inspections confirmed that the aircraft was airworthy and that the control surfaces and linkages were fully functional at the time of the accident. The investigation also attempted to retrieve flight data from the onboard LX 7007 PRO IGC and Universal Sensor Box-D, but the recording media were found to be destroyed by the impact.

Findings

  • The glider entered a stall, most likely at a low airspeed.
  • The pilot used recovery techniques that contradicted the manufacturer's flight manual, which advises slightly pushing the control stick forward during a low-speed stall rather than pulling back.
  • The pilot had limited experience specifically with the DG-400 model.

Probable cause

The accident was caused by the pilot's use of incorrect recovery techniques during a low-speed stall, specifically pulling back on the control stick instead of following the flight manual's recommendation to push forward.

Frequently asked questions

What happened in the 2011-08-14 DG 400 accident near NNW obce Bystřice (okres Benešov), CZ?

A pilot was forced to bail out of a DG-400 glider after the aircraft entered an unrecoverable descent during thermal soaring.

What aircraft was involved and where did it happen?

The accident on 2011-08-14 involved a DG 400, registration OK-2154, at NNW obce Bystřice (okres Benešov), CZ.

What was the probable cause of the accident?

The accident was caused by the pilot's use of incorrect recovery techniques during a low-speed stall, specifically pulling back on the control stick instead of following the flight manual's recommendation to push forward.

Investigation report by the Czech Air Accidents Investigation Institute (UZPLN). Original record: https://uzpln.gov.cz/incident/272. This page is a structured re-presentation; facts and quotes are in the Ustav pro odborne zjistovani pricin leteckych nehod (UZPLN), Czech Republic.

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