Engine Failure During Go-Around Leads to Off-Runway Impact

Casualties unknown • Chandler, AZ, US

An engine failure occurred during a go-around at approximately 100 feet, resulting in the aircraft impacting a berm, tree, and light post after landing in an off-runway field.

What happened

During a go-around maneuver at approximately 100 feet above ground level, the pilot applied full power and engaged the carburetor heat. At that moment, the engine ceased operation completely without any preceding coughing or sputtering.

The pilot reported that the aircraft's heading was approximately 15 degrees off from the runway heading. The aircraft subsequently touched down in a field, where it struck a berm, a tree, and a light post.

During recovery operations, as the aircraft was being trailered back to the airport, a steady stream of fuel was observed flowing from the bottom fuel sump. Upon moving the aircraft to another location, approximately 1 gallon of fuel was found remaining in the tanks.

The investigation

An examination of the engine and fuel system components was performed following the recovery of the aircraft. Investigators found no mechanical discrepancies within the engine or the fuel system components. However, dark sooty deposits were identified within the carburetor throat. It was noted that the carburetor in use does not feature an accelerator pump.

Probable cause

The engine failure occurred when the pilot applied full power and engaged carburetor heat during a go-around.

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Frequently asked questions

What happened in the 1999-05-08 Cessna 152 accident near Chandler, AZ?

An engine failure occurred during a go-around at approximately 100 feet, resulting in the aircraft impacting a berm, tree, and light post after landing in an off-runway field.

What aircraft was involved and where did it happen?

The accident on 1999-05-08 involved a Cessna 152, registration N48845, operated by South Bay Aviation, at Chandler, AZ.

What was the probable cause of the accident?

The engine failure occurred when the pilot applied full power and engaged carburetor heat during a go-around.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20001212X18804. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

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