CRJ-200 landing accident during instrument approach

Casualties unknown • Providence, RI, US

A CRJ-200 experienced a high sink rate and landing gear failure during an approach to Providence due to pilot error and inadequate training oversight.

What happened

The flight crew was performing a straight-in ILS approach under instrument meteorological conditions, with cloud ceilings approximately 10-foot above the decision height. The aircraft was experiencing tailwinds of up to 100 knots, which resulted in high ground speeds that caused the crew to feel rushed. While the CRJ-200 was established on the correct course, altitude, and speed, the crew failed to perform a complete approach briefing.

The first officer, who had limited experience with this aircraft type, disengaged the autopilot and flight director but only verbally communicated the autopilot disconnection. The aircraft subsequently drifted left of the course and above the glidepath, resulting in an unstabilized approach. As the aircraft descended below the ceiling, the pilots noticed the deviation.

The captain attempted to take control to salvage the landing rather than executing a missed approach. During this transition, the first officer misunderstood a statement from the captain and reduced power to idle without notifying him. This caused the aircraft to develop a high sink rate. During the flare, the aircraft likely stalled and impacted the runway with a high vertical rate. The impact forces exceeded the certified limits of the landing gear, causing the gear support trunnion to fracture.

There were no fatalities reported in this accident.

The investigation

The investigation examined the mechanical integrity of the landing gear and found no evidence of pre-existing damage; the gear separation occurred as designed due to the impact loads. Investigators also reviewed Air Wisconsin's training and oversight programs. It was noted that simulator time requirements for new-hire pilots had been reduced, and the company's reliance on increased initial operating experience (IOE) was not an adequate substitute for simulator training. Furthermore, the investigation found that the airline lacked effective methods to assess the performance of probationary first officers, as trip reports were not being produced and progress meetings had been discontinued.

Findings

  • The first officer's training and checkrides failed to identify weaknesses in automation use, pacing, and crew coordination.
  • The company's training program did not adequately accommodate the needs of less experienced first officers.
  • Inadequate training and oversight contributed to the pilot's inability to properly execute the approach.

Probable cause

The accident was caused by the first officer's reduction of power to idle without the captain's knowledge during a manual takeover, leading to a high sink rate and subsequent stall and impact.

Frequently asked questions

What happened in the 2007-12-16 Bombardier CL600-2B19 accident near Providence, RI?

A CRJ-200 experienced a high sink rate and landing gear failure during an approach to Providence due to pilot error and inadequate training oversight.

What aircraft was involved and where did it happen?

The accident on 2007-12-16 involved a Bombardier CL600-2B19, registration N470ZW, operated by Air Wisconsin Airlines, at Providence, RI.

What was the probable cause of the accident?

The accident was caused by the first officer's reduction of power to idle without the captain's knowledge during a manual takeover, leading to a high sink rate and subsequent stall and impact.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20071217X01939. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

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