Electrical malfunction during taxiing at Warsaw Chopin Airport

Casualties unknown • EPWA, PL

Smoke and a burning smell were detected in the cockpit of a Let L-410 Turbolet during taxiing for a ground navigation test flight.

What happened

On August 24, 2016, an L-410 Turbolet was taxiing at Warsaw Chopin Airport (EPWA) in preparation for a ground-based navigation equipment test flight. During the taxiing phase, the crew observed smoke emerging from the left side of the cockpit, accompanied by the smell of burning.

In response to the smoke, the crew immediately decided to abort the taxiing procedure and returned the aircraft to its parking position. Following the incident, maintenance personnel conducted a thorough inspection of the aircraft's electrical system.

The investigation

The investigation focused on identifying the source of the smoke and the burning odor within the cockpit area. Technical personnel examined the electrical installations and identified a failure in the instrument panel lighting control component. Specifically, the investigation established that the winding of a potentiometer, used to regulate the brightness of the instrument panel illumination, had burned out.

Findings

  • The primary cause of the incident was the burning of the potentiometer winding.
  • The failure was most likely caused by operational wear and tear of the component.
  • Following the replacement of the faulty potentiometer and subsequent functional testing, the aircraft was cleared for continued operation.

Probable cause

The electrical malfunction was caused by the failure of a potentiometer winding due to normal operational wear.

Frequently asked questions

What happened in the 2016-08-24 LET, L-410 Turbolet accident near EPWA, PL?

Smoke and a burning smell were detected in the cockpit of a Let L-410 Turbolet during taxiing for a ground navigation test flight.

What aircraft was involved and where did it happen?

The accident on 2016-08-24 involved a LET, L-410 Turbolet, at EPWA, PL.

What was the probable cause of the accident?

The electrical malfunction was caused by the failure of a potentiometer winding due to normal operational wear.

Investigation report by the Polish State Commission on Aircraft Accidents Investigation (PKBWL). Original record: https://pkbwl.gov.pl/raporty/2016-2220/. This page is a structured re-presentation; facts and quotes are in the Panstwowa Komisja Badania Wypadkow Lotniczych (PKBWL), Poland.

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