1989-07-13: Piper J-3 — Wilkinson, Robert — Parker Lake, AK

Casualties unknown • Parker Lake, AK, US

Probable cause

IMPROPER PREFLIGHT PLANNING BY THE PILOT AND HIS FAILURE TO ATTAIN AND/OR MAINTAIN ADEQUATE SPEED, WHICH RESULTED IN A STALL/MUSH AFTER LIFT-OFF.

— NTSB Determination

Accident narrative

THE PLT RPRTD THAT DRG TAKEOFF FROM A LAKE, THE ACFT FLEW APRX 200 FT, THEN SETTLED IN A SWAMP. IN A STATEMENT AFTER THE ACDNT, HE NOTED HE HAD 'EXCESSIVE BACK PRESSURE' ON THE CONTROL STICK & STATED THAT MORE SPEED AT LIFT-OFF WOULD HAVE BEEN HELPFUL. ALSO, HE RPRTD THERE WERE CALM WIND CONDITIONS & RAIN SHOWERS IN THE AREA. THERE WAS ANOTHER PART ON THE LAKE THAT WOULD HAVE PROVIDED A LONGER TAKEOFF AREA.

Frequently asked questions

What happened in the 1989-07-13 Piper J-3 accident near Parker Lake, AK?

THE PLT RPRTD THAT DRG TAKEOFF FROM A LAKE, THE ACFT FLEW APRX 200 FT, THEN SETTLED IN A SWAMP. IN A STATEMENT AFTER THE ACDNT, HE NOTED HE HAD 'EXCESSIVE BACK PRESSURE' ON THE CONTROL STICK & STATED THAT MORE SPEED AT LIFT-OFF WOULD HAVE BEEN HELPFUL. ALSO, HE RPRTD THERE WERE CALM WIND CONDITIONS & RAIN SHOWERS IN…

What aircraft was involved and where did it happen?

The accident on 1989-07-13 involved a Piper J-3, registration N27024, operated by Wilkinson, Robert, at Parker Lake, AK.

What was the probable cause of the accident?

IMPROPER PREFLIGHT PLANNING BY THE PILOT AND HIS FAILURE TO ATTAIN AND/OR MAINTAIN ADEQUATE SPEED, WHICH RESULTED IN A STALL/MUSH AFTER LIFT-OFF.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20001213X28700. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

Loading the flight search…