1990-08-24: Piper PA-32RT-300 — Larry W. Biggs — Hattiesburg, MS

Casualties unknown • Hattiesburg, MS, US

Probable cause

FAILURE OF THE PILOT IN COMMAND TO ATTAIN ADEQUATE AIRSPEED PRIOR TO LIFTOFF DURING AN ATTEMPTED TAKEOFF. THE PILOT THEN LOST CONTROL OF THE AIRPLANE IN FLIGHT. THE PILOT ALSO DELAYED IN HIS DECISION TO ABORT THE TAKEOFF.

— NTSB Determination

Accident narrative

THE PILOT ATTEMPTED A TAKEOFF AND NOTED AT LIFTOFF THAT THE AIRPLANE WAS YAWING TO THE LEFT AND HIS ATTEMPTS TO USE RIGHT RUDDER IMPUTS WERE INEFFECTIVE. HE LET THE AIRPLANE DRIFT 400 FEET TO THE LEFT OF THE RUNWAY WITH THE GEAR STILL DOWN AND THEN REDUCED POWER AND CRASHED. NO FAILURES OR MIS-RIGGING OF THE FLIGHT CONTROLS WERE FOUND.

Frequently asked questions

What happened in the 1990-08-24 Piper PA-32RT-300 accident near Hattiesburg, MS?

THE PILOT ATTEMPTED A TAKEOFF AND NOTED AT LIFTOFF THAT THE AIRPLANE WAS YAWING TO THE LEFT AND HIS ATTEMPTS TO USE RIGHT RUDDER IMPUTS WERE INEFFECTIVE. HE LET THE AIRPLANE DRIFT 400 FEET TO THE LEFT OF THE RUNWAY WITH THE GEAR STILL DOWN AND THEN REDUCED POWER AND CRASHED. NO FAILURES OR MIS-RIGGING OF THE FLIGHT…

What aircraft was involved and where did it happen?

The accident on 1990-08-24 involved a Piper PA-32RT-300, registration N289PC, operated by Larry W. Biggs, at Hattiesburg, MS.

What was the probable cause of the accident?

FAILURE OF THE PILOT IN COMMAND TO ATTAIN ADEQUATE AIRSPEED PRIOR TO LIFTOFF DURING AN ATTEMPTED TAKEOFF. THE PILOT THEN LOST CONTROL OF THE AIRPLANE IN FLIGHT. THE PILOT ALSO DELAYED IN HIS DECISION TO ABORT THE TAKEOFF.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20001212X24083. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

Loading the flight search…