1991-01-02: Hughes 269C — Maverick Helicopters, Inc. — Deland, FL

Casualties unknown • Deland, FL, US

Probable cause

FAILURE OF THE COMMERCIAL PILOT APPLICANT TO PULL COLLECTIVE PITCH AND DELAY BY THE CHECK AIRMAN TO PULL COLLECTIVE AND APPLY POWER TO RECOVER, RESULTING IN A HARD LANDING.

— NTSB Determination

Accident narrative

DURING A COMMERCIAL PLT CHECK RIDE, THE CHECK AIRMAN REDUCED THE THROTTLE TO IDLE TO SIMULATE AN ENG FAILURE. THE APPLICANT ENTERED AN AUTOROTATIVE LANDING & WAS ADVISED THAT THE MANEUVER WOULD BE COMPLETED TO A 3-FOOT HOVER. AT 6 FT AGL, THE APPLICANT DID NOT PULL COLLECTIVE PITCH NOR APPLY POWER. THE CFI TOOK CONTROL & APPLIED COLLECTIVE PITCH & POWER BUT THE DESCENT CONTINUED & THE HELICOPTER TOUCHED DOWN, BOUNCED, WAS RECOVERED TO A HOVER, & LANDED WITH NO FURTHER INCIDENT.

Frequently asked questions

What happened in the 1991-01-02 Hughes 269C accident near Deland, FL?

DURING A COMMERCIAL PLT CHECK RIDE, THE CHECK AIRMAN REDUCED THE THROTTLE TO IDLE TO SIMULATE AN ENG FAILURE. THE APPLICANT ENTERED AN AUTOROTATIVE LANDING & WAS ADVISED THAT THE MANEUVER WOULD BE COMPLETED TO A 3-FOOT HOVER. AT 6 FT AGL, THE APPLICANT DID NOT PULL COLLECTIVE PITCH NOR APPLY POWER. THE CFI TOOK…

What aircraft was involved and where did it happen?

The accident on 1991-01-02 involved a Hughes 269C, registration N9574F, operated by Maverick Helicopters, Inc., at Deland, FL.

What was the probable cause of the accident?

FAILURE OF THE COMMERCIAL PILOT APPLICANT TO PULL COLLECTIVE PITCH AND DELAY BY THE CHECK AIRMAN TO PULL COLLECTIVE AND APPLY POWER TO RECOVER, RESULTING IN A HARD LANDING.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20001212X16350. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

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