1992-06-30: Cessna 180 — Arthur W. Utay — Glendale, AZ

Casualties unknown • Glendale, AZ, US

Probable cause

THE FAILURE OF THE LEFT MAIN GEAR INNER TUBE DUE TO DRY ROT, AND, THE INADEQUATE MAINTENANCE AND PREFLIGHT INSPECTIONS CONDUCTED ON THE AIRCRAFT.

— NTSB Determination

Accident narrative

THE AIRCRAFT GROUND LOOPED AFTER TOUCHDOWN. THE PILOT REPORTED THAT THE LEFT MAIN GEAR TIRE SUSTAINED A BLOW OUT AND HE LOST DIRECTIONAL CONTROL. INVESTIGATION REVEALED THAT THE LEFT WHEEL TUBE VALVE STEM BROKE OFF AT THE BASE DUE TO DRY ROT. THE TUBE REPORTEDLY HAD 1,200 HOURS SINCE NEW. THE AIRCRAFT HAD AN ANNUAL INSPECTION 7 HOURS AND ONE MONTH PRIOR TO THE ACCIDENT.

Frequently asked questions

What happened in the 1992-06-30 Cessna 180 accident near Glendale, AZ?

THE AIRCRAFT GROUND LOOPED AFTER TOUCHDOWN. THE PILOT REPORTED THAT THE LEFT MAIN GEAR TIRE SUSTAINED A BLOW OUT AND HE LOST DIRECTIONAL CONTROL. INVESTIGATION REVEALED THAT THE LEFT WHEEL TUBE VALVE STEM BROKE OFF AT THE BASE DUE TO DRY ROT. THE TUBE REPORTEDLY HAD 1,200 HOURS SINCE NEW. THE AIRCRAFT HAD AN ANNUAL…

What aircraft was involved and where did it happen?

The accident on 1992-06-30 involved a Cessna 180, registration N2362C, operated by Arthur W. Utay, at Glendale, AZ.

What was the probable cause of the accident?

THE FAILURE OF THE LEFT MAIN GEAR INNER TUBE DUE TO DRY ROT, AND, THE INADEQUATE MAINTENANCE AND PREFLIGHT INSPECTIONS CONDUCTED ON THE AIRCRAFT.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20001211X14921. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

Loading the flight search…