1992-07-25: Stinson 108-3 — J.d. Twenter — Boonville, MO

Casualties unknown • Boonville, MO, US

Probable cause

INADEQUATE PREFLIGHT PLANNING, AND EXCEEDING THE PERFORMANCE CAPABILITY OF THE AIRPLANE BY THE PILOT-IN-COMMAND.

— NTSB Determination

Accident narrative

THE AIRPLANE STRUCK POWER LINES NEAR DEPARTURE END OF RUNWAY AND CRASHED INTO A PARKING LOT AND WAS DESTROYED BY A POST CRASH FIRE. THE AIRPLANE HAD FULL FUEL, THREE PASSENGERS, AND 100 HUNDRED POUNDS OF BAGGAGE. THE RUNWAY WAS 2600 FEET LONG, THE SURFACE WAS LONG GRASS, AND THE GROUND WAS SOFT AND UNEVEN. THE AIRPLANE WAS APPROXIMATELY 175 POUNDS OVER MAXIMUM GROSS WEIGHT. TAKEOFF DISTANCE REQUIRED FOR 50 FOOT OBSTACLE CLEARANCE WAS 3188 FEET.

Frequently asked questions

What happened in the 1992-07-25 Stinson 108-3 accident near Boonville, MO?

THE AIRPLANE STRUCK POWER LINES NEAR DEPARTURE END OF RUNWAY AND CRASHED INTO A PARKING LOT AND WAS DESTROYED BY A POST CRASH FIRE. THE AIRPLANE HAD FULL FUEL, THREE PASSENGERS, AND 100 HUNDRED POUNDS OF BAGGAGE. THE RUNWAY WAS 2600 FEET LONG, THE SURFACE WAS LONG GRASS, AND THE GROUND WAS SOFT AND UNEVEN. THE…

What aircraft was involved and where did it happen?

The accident on 1992-07-25 involved a Stinson 108-3, registration N948C, operated by J.d. Twenter, at Boonville, MO.

What was the probable cause of the accident?

INADEQUATE PREFLIGHT PLANNING, AND EXCEEDING THE PERFORMANCE CAPABILITY OF THE AIRPLANE BY THE PILOT-IN-COMMAND.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20001211X15102. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

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