1992-12-23: Cessna 180K — Woodruff, Harold S. ET AL — Fullerton, CA

Casualties unknown • Fullerton, CA, US

Probable cause

THE AIRPLANE'S OWNERS (INCLUDING THE PILOT) POOR MAINTENANCE AND THE PILOT'S INADEQUATE PREFLIGHT INSPECTION. CONTRIBUTING TO THIS ACCIDENT WAS THE DETERIORATED OVERWING FUEL CAPS SEALS AND THE TAILWIND.

— NTSB Determination

Accident narrative

THE PILOT DRAINED OUT MULTIPLE FUEL TESTER TUBES OF WATER BEFORE DEPARTING ON THE ACCIDENT FLIGHT. SHORTLY AFTER LIFT OFF THE ENGINE EXPERIENCED AN INTERMITTENT LOSS OF POWER. THE PILOT RETURNED TO THE DEPARTURE AIRPORT AND LANDED DOWNWIND, BEYOND MIDFIELD. THE AIRPLANE OVERRAN THE RUNWAY ENVIRONMENT AND COLLIDED WITH THE AIRPORT PERIMETER FENCE. EXAMINATION OF THE WRECKAGE REVEALED CONSIDERABLE WATER REMAINED IN THE FUEL TANKS AND THE OVERWING FUEL CAP SEALS WERE DETERIORATED.

Frequently asked questions

What happened in the 1992-12-23 Cessna 180K accident near Fullerton, CA?

THE PILOT DRAINED OUT MULTIPLE FUEL TESTER TUBES OF WATER BEFORE DEPARTING ON THE ACCIDENT FLIGHT. SHORTLY AFTER LIFT OFF THE ENGINE EXPERIENCED AN INTERMITTENT LOSS OF POWER. THE PILOT RETURNED TO THE DEPARTURE AIRPORT AND LANDED DOWNWIND, BEYOND MIDFIELD. THE AIRPLANE OVERRAN THE RUNWAY ENVIRONMENT AND COLLIDED…

What aircraft was involved and where did it happen?

The accident on 1992-12-23 involved a Cessna 180K, registration N61798, operated by Woodruff, Harold S. ET AL, at Fullerton, CA.

What was the probable cause of the accident?

THE AIRPLANE'S OWNERS (INCLUDING THE PILOT) POOR MAINTENANCE AND THE PILOT'S INADEQUATE PREFLIGHT INSPECTION. CONTRIBUTING TO THIS ACCIDENT WAS THE DETERIORATED OVERWING FUEL CAPS SEALS AND THE TAILWIND.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20001211X16187. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

Loading the flight search…