1993-03-03: Piper PA-32-260 — Karl T. Lieb — Riverton, WY

Casualties unknown • Riverton, WY, US

Probable cause

THE PILOT DID NOT PERFORM AN ABORT OF THE TAKEOFF AFTER OBSERVING A PARTIAL LOSS OF POWER. FACTORS INCLUDE IMPROPER USE OF THE MIXTURE CONTROL.

— NTSB Determination

Accident narrative

THE PILOT OBSERVED THAT THE AIRCRAFT WAS NOT PRODUCING EXPECTED POWER, AND ASSURED DURING THE TAKEOFF GROUND RUN THAT THE PROPELLER, THROTTLE, AND MIXTURE CONTROLS WERE FULL FORWARD. THE TAKEOFF USED ABOUT HALF THE LENGTH OF THE 8202 FOOT RUNWAY. THE AIRCRAFT LIFTED OFF, CLIMBED TO ABOUT 50 FEET AND WOULD NOT CLIMB. THE AIRCRAFT STRUCK A LIGHT POLE AND CRASHED IN A FIELD ABOUT 1.5 MILES FROM THE AIRPORT. ALTHOUGH THE PILOT NOTED THAT HE HAD EXPECTED TO TAKEOFF GROUND RUN TO BE ABOUT 2000 FEET, HE FAILED TO ABORT THE TAKEOFF.

Frequently asked questions

What happened in the 1993-03-03 Piper PA-32-260 accident near Riverton, WY?

THE PILOT OBSERVED THAT THE AIRCRAFT WAS NOT PRODUCING EXPECTED POWER, AND ASSURED DURING THE TAKEOFF GROUND RUN THAT THE PROPELLER, THROTTLE, AND MIXTURE CONTROLS WERE FULL FORWARD. THE TAKEOFF USED ABOUT HALF THE LENGTH OF THE 8202 FOOT RUNWAY. THE AIRCRAFT LIFTED OFF, CLIMBED TO ABOUT 50 FEET AND WOULD NOT CLIMB.…

What aircraft was involved and where did it happen?

The accident on 1993-03-03 involved a Piper PA-32-260, registration N821SC, operated by Karl T. Lieb, at Riverton, WY.

What was the probable cause of the accident?

THE PILOT DID NOT PERFORM AN ABORT OF THE TAKEOFF AFTER OBSERVING A PARTIAL LOSS OF POWER. FACTORS INCLUDE IMPROPER USE OF THE MIXTURE CONTROL.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20001211X12040. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

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