1993-08-15: Piper J-3C-85 — Dahl, David & Michael — Salol, MN

Casualties unknown • Salol, MN, US

Probable cause

THE PILOT'S FAILURE TO MAINTAIN ADEQUATE AIRSPEED RESULTING IN AN AERODYNAMIC STALL. THE PILOT'S LACK OF RECENT FLIGHT EXPERIENCE IS A RELATED FACTOR.

— NTSB Determination

Accident narrative

THE PURPOSE OF THE FLIGHT WAS AERIAL OBSERVATION OF A WHEAT FIELD. WITNESSES OBSERVED THE AIRPLANE MANEUVERING AT LOW ALTITUDES (LESS THAN 100 FEET AGL), BEFORE IT PITCHED NOSE UP AND BANKED TO THE LEFT INTO THE GROUND. A POSTIMPACT FIRE ENSUED. POSTACCIDENT INVESTIGATION REVEALED NO EVIDENCE OF PREIMPACT MECHANICAL MALFUNCTION. RECORDS INDICATE THE PILOT HAD APPROXIMATELY 435 HOURS TOTAL FLIGHT TIME, OF WHICH ABOUT 390 HOURS WERE IN THE ACCIDENT AIRPLANE. THE AIRPLANE CO-OWNER STATED THE PILOT HAD FLOWN LESS THAN TWO HOURS IN THE PRECEDING EIGHT MONTHS.

Frequently asked questions

What happened in the 1993-08-15 Piper J-3C-85 accident near Salol, MN?

THE PURPOSE OF THE FLIGHT WAS AERIAL OBSERVATION OF A WHEAT FIELD. WITNESSES OBSERVED THE AIRPLANE MANEUVERING AT LOW ALTITUDES (LESS THAN 100 FEET AGL), BEFORE IT PITCHED NOSE UP AND BANKED TO THE LEFT INTO THE GROUND. A POSTIMPACT FIRE ENSUED. POSTACCIDENT INVESTIGATION REVEALED NO EVIDENCE OF PREIMPACT MECHANICAL…

What aircraft was involved and where did it happen?

The accident on 1993-08-15 involved a Piper J-3C-85, registration N6301H, operated by Dahl, David & Michael, at Salol, MN.

What was the probable cause of the accident?

THE PILOT'S FAILURE TO MAINTAIN ADEQUATE AIRSPEED RESULTING IN AN AERODYNAMIC STALL. THE PILOT'S LACK OF RECENT FLIGHT EXPERIENCE IS A RELATED FACTOR.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20001211X13084. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

Loading the flight search…