1994-03-30: Cessna 180 — Austin, TX

Casualties unknown • Austin, TX, US

Probable cause

THE LOSS OF ENGINE POWER FOR UNDETERMINED REASONS. FACTORS WERE THE WIRE STRIKE AND LACK OF SUITABLE TERRAIN.

— NTSB Determination

Accident narrative

FOLLOWING THE LOSS OF ENGINE POWER THE PILOT SWITCHED FUEL SELECTORS FROM THE BOTH POSITION TO THE LEFT TANK AND ATTEMPTED AN ENGINE RESTART. DURING THE FORCED LANDING THE AIRCRAFT STRUCK A POWER LINE AND DESCENDED OUT OF CONTROL TO GROUND IMPACTED .25 MILES SHORT OF THE THRESHOLD. AN EXAMINATION OF THE AIRCRAFT REVEALED THAT THE RIGHT TANK CONTAINED 2.5 GALLONS OF FUEL AND THE LEFT TANK 6.5 GALLONS OF FUEL. TWO AND ONE HALF GALLONS IN EACH TANK IS UNUSABLE.

Frequently asked questions

What happened in the 1994-03-30 Cessna 180 accident near Austin, TX?

FOLLOWING THE LOSS OF ENGINE POWER THE PILOT SWITCHED FUEL SELECTORS FROM THE BOTH POSITION TO THE LEFT TANK AND ATTEMPTED AN ENGINE RESTART. DURING THE FORCED LANDING THE AIRCRAFT STRUCK A POWER LINE AND DESCENDED OUT OF CONTROL TO GROUND IMPACTED .25 MILES SHORT OF THE THRESHOLD. AN EXAMINATION OF THE AIRCRAFT…

What aircraft was involved and where did it happen?

The accident on 1994-03-30 involved a Cessna 180, registration N4646B, at Austin, TX.

What was the probable cause of the accident?

THE LOSS OF ENGINE POWER FOR UNDETERMINED REASONS. FACTORS WERE THE WIRE STRIKE AND LACK OF SUITABLE TERRAIN.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20001206X00913. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

Loading the flight search…