Nose gear extension failure due to incorrect steering system rigging

Casualties unknown • Charlotte, NC, US

An aircraft was forced to land with its nose gear not down and locked after mechanical issues prevented proper extension during the landing sequence.

What happened

During the landing phase of flight, the flightcrew attempted to extend the landing gear but observed that the nose gear failed to provide a "down and locked" indication. The crew made several additional attempts to lower the nose gear, but these efforts were unsuccessful. As a result, the aircraft was landed with the nose gear not down and locked.

The investigation

Post-flight inspections of the aircraft revealed that the nosewheel steering system had been incorrectly rigged. Specifically, the nose gear failed to properly center itself, and the tensions in the nosewheel steering cables were found to be below the required limits. This mechanical condition caused the nose gear to strike the side wall of the gear well, which physically prevented the gear from extending fully.

The investigation also noted that approximately two weeks before the incident, the nosewheel steering control valve had been replaced. This maintenance procedure would have necessitated a subsequent check of the nose gear rigging.

Probable cause

The nose gear failed to extend because the nosewheel steering system was incorrectly rigged and cable tensions were below limits, causing the gear to hit the side wall of the gear well; this condition followed the replacement of the nosewheel steering control valve without a proper rigging check.

Frequently asked questions

What happened in the 1994-05-01 Fokker F28 MK 0100 accident near Charlotte, NC?

An aircraft was forced to land with its nose gear not down and locked after mechanical issues prevented proper extension during the landing sequence.

What aircraft was involved and where did it happen?

The accident on 1994-05-01 involved a Fokker F28 MK 0100, registration N890US, operated by Usair, Inc., at Charlotte, NC.

What was the probable cause of the accident?

The nose gear failed to extend because the nosewheel steering system was incorrectly rigged and cable tensions were below limits, causing the gear to hit the side wall of the gear well; this condition followed the replacement of the nosewheel steering control valve without a proper rigging check.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20001206X01204. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

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