1994-08-04: Stinson 108 — Loomis, Andrew D. — Salcha, AK

Casualties unknown • Salcha, AK, US

Probable cause

THE PILOT DID NOT MAINTAIN CONTROL OF THE AIRPLANE. A FACTOR IN THE ACCIDENT WAS THE PILOT'S LACK OF TOTAL EXPERIENCE IN THE SPECIFIC MAKE/MODEL/TYPE OF AIRCRAFT.

— NTSB Determination

Accident narrative

THE PRIVATE PILOT WITH 65 TOTAL FLIGHT HOURS AND 4.8 HOURS IN THE SPECIFIC MAKE/MODEL WAS ATTEMPTING TO LAND HIS AIRPLANE AT A PRIVATE GRASS STRIP. ON INITIAL TOUCHDOWN, THE AIRPLANE BOUNCED INTO THE AIR. THE PLANE'S LEFT WING STRUCK SOME BRUSH AND THE MAIN LANDING GEAR CONTACTED THE RUNWAY AGAIN. THE PILOT REDUCED THE PLANE'S ENGINE POWER TO IDLE AND APPLIED THE WHEEL BRAKES AT WHICH TIME THE PLANE NOSED OVER.

Frequently asked questions

What happened in the 1994-08-04 Stinson 108 accident near Salcha, AK?

THE PRIVATE PILOT WITH 65 TOTAL FLIGHT HOURS AND 4.8 HOURS IN THE SPECIFIC MAKE/MODEL WAS ATTEMPTING TO LAND HIS AIRPLANE AT A PRIVATE GRASS STRIP. ON INITIAL TOUCHDOWN, THE AIRPLANE BOUNCED INTO THE AIR. THE PLANE'S LEFT WING STRUCK SOME BRUSH AND THE MAIN LANDING GEAR CONTACTED THE RUNWAY AGAIN. THE PILOT REDUCED…

What aircraft was involved and where did it happen?

The accident on 1994-08-04 involved a Stinson 108, registration N97294, operated by Loomis, Andrew D., at Salcha, AK.

What was the probable cause of the accident?

THE PILOT DID NOT MAINTAIN CONTROL OF THE AIRPLANE. A FACTOR IN THE ACCIDENT WAS THE PILOT'S LACK OF TOTAL EXPERIENCE IN THE SPECIFIC MAKE/MODEL/TYPE OF AIRCRAFT.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20001206X01910. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

Loading the flight search…