1994-10-01: Cessna 180 — Hall, Wayne — Aniak, AK

Casualties unknown • Aniak, AK, US

Probable cause

THE PILOT'S FAILURE TO MAINTAIN PROPER RUNWAY ALIGNMENT DURING THE TAKEOFF ROLL. A FACTOR ASSOCIATED WITH THE ACCIDENT WAS THE ROUGH/UNEVEN CONDITION OF THE RUNWAY'S SURFACE.

— NTSB Determination

Accident narrative

THE FLIGHT WAS DEPARTING AN AIRSTRIP THAT WAS IN POOR CONDITION. THE PILOT STATED THE LEFT MAIN GEAR 'SLIPPED' INTO A DEPRESSION IN THE RUNWAY'S SURFACE DURING THE TAKEOFF ROLL. THE AIRPLANE CONTINUED TO SLIP OFF THE RUNWAY UNTIL THE LEFT WHEEL STRUCK THE WILLOWS GROWING ON THE RUNWAY'S EDGE. THE PILOT STATED IT WAS TOO LATE TO ABORT THE TAKEOFF AND THE AIRPLANE OVERRAN THE END OF THE RUNWAY.

Frequently asked questions

What happened in the 1994-10-01 Cessna 180 accident near Aniak, AK?

THE FLIGHT WAS DEPARTING AN AIRSTRIP THAT WAS IN POOR CONDITION. THE PILOT STATED THE LEFT MAIN GEAR 'SLIPPED' INTO A DEPRESSION IN THE RUNWAY'S SURFACE DURING THE TAKEOFF ROLL. THE AIRPLANE CONTINUED TO SLIP OFF THE RUNWAY UNTIL THE LEFT WHEEL STRUCK THE WILLOWS GROWING ON THE RUNWAY'S EDGE. THE PILOT STATED IT WAS…

What aircraft was involved and where did it happen?

The accident on 1994-10-01 involved a Cessna 180, registration N2707X, operated by Hall, Wayne, at Aniak, AK.

What was the probable cause of the accident?

THE PILOT'S FAILURE TO MAINTAIN PROPER RUNWAY ALIGNMENT DURING THE TAKEOFF ROLL. A FACTOR ASSOCIATED WITH THE ACCIDENT WAS THE ROUGH/UNEVEN CONDITION OF THE RUNWAY'S SURFACE.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20001206X02368. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

Loading the flight search…