1995-07-07: Stinson 108-2 — Anchorage, AK

Casualties unknown • Anchorage, AK, US

Probable cause

THE PILOT'S LOSS OF DIRECTIONAL CONTROL, DURING THE TAKEOFF ROLL, WHICH RESULTED IN AN INADVERTENT SWERVE, AND THE PILOT'S EXCESSIVE APPLICATION OF BRAKE PRESSURE, WHICH RESULTED IN A NOSE DOWN CONDITION.

— NTSB Determination

Accident narrative

THE AIRPLANE VEERED TO THE LEFT DURING THE FIRST ATTEMPT TO TAKE OFF. THE PILOT STATED SHE ATTRIBUTED THIS TO WIND GUSTS FROM THE WEST (LEFT). DURING THE SECOND ATTEMPT TO TAKE OFF, THE AIRPLANE VEERED TO THE LEFT AGAIN AND DEPARTED THE LEFT SIDE OF THE RUNWAY, TOWARD SOME PARKED AIRCRAFT. THE PILOT APPLIED THE BRAKES, AND THE AIRPLANE NOSED DOWN. THE WINDS WERE REPORTED TO BE FROM 310 DEGREES AT 4 KNOTS.

Frequently asked questions

What happened in the 1995-07-07 Stinson 108-2 accident near Anchorage, AK?

THE AIRPLANE VEERED TO THE LEFT DURING THE FIRST ATTEMPT TO TAKE OFF. THE PILOT STATED SHE ATTRIBUTED THIS TO WIND GUSTS FROM THE WEST (LEFT). DURING THE SECOND ATTEMPT TO TAKE OFF, THE AIRPLANE VEERED TO THE LEFT AGAIN AND DEPARTED THE LEFT SIDE OF THE RUNWAY, TOWARD SOME PARKED AIRCRAFT. THE PILOT APPLIED THE…

What aircraft was involved and where did it happen?

The accident on 1995-07-07 involved a Stinson 108-2, registration N257C, at Anchorage, AK.

What was the probable cause of the accident?

THE PILOT'S LOSS OF DIRECTIONAL CONTROL, DURING THE TAKEOFF ROLL, WHICH RESULTED IN AN INADVERTENT SWERVE, AND THE PILOT'S EXCESSIVE APPLICATION OF BRAKE PRESSURE, WHICH RESULTED IN A NOSE DOWN CONDITION.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20001207X03834. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

Loading the flight search…