Takeoff Rejected Following Sudden Directional Swing at Manchester Airport

Casualties unknown • Manchester Airport, GB

A Boeing 737-300 experienced a rapid rightward swing during takeoff at Manchester Airport, leading the flight crew to abort the departure.

What happened

On 19 October 2009, a Boeing 737-300, registration G-CELI, was preparing for a commercial passenger flight from Manchester Airport to Budapest. During the takeoff roll on Runway 23 Right, the aircraft reached a speed of approximately 83 knots when it experienced a sudden and violent swing to the right. The flight crew, noticing the deviation, immediately rejected the takeoff. The aircraft approached the edge of the runway, requiring a combination of nosewheel steering and rudder inputs to return to the centerline, before coming to a stop. The airport fire service attended the scene, and all 119 passengers and 5 crew members were safely disembarking without injury.

The investigation

The AAIB investigation focused on the cause of the sudden lateral movement. While the flight crew did not recall making a significant rudder input, Flight Data Recorder (FDR) analysis revealed a large right rudder pedal input occurred just before the swing. This was followed by a large left rudder input as the crew attempted to correct the heading. A manufacturer-led desktop simulation confirmed that the aircraft's behavior, including the recorded lateral acceleration, was consistent with the observed rudder pedal movements.

Investigators also reviewed the maintenance history of G-CELI, noting a pattern of directional control issues during landing rolls in previous months. While a leaking steering metering valve was identified and subsequently replaced, testing indicated this leak was not significant enough to cause the takeoff incident. Further inspections of the braking, flap, and tire systems revealed no faults.

Findings

  • The sudden rightward swing was caused by a large right rudder pedal input.
  • Flight recorder data showed the rudder deflected to full travel, despite the crew not recalling such an input.
  • The aircraft had a documented history of intermittent directional control difficulties, though these were previously noted only during the landing phase.
  • A leaking steering metering valve was discovered, but it was not determined to be the cause of the takeoff excursion.

Probable cause

The sudden deviation from the runway centerline was caused by a large, unexpected right rudder pedal input, which the flight crew did not recall performing.

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Frequently asked questions

What happened in the 2009-10-19 Boeing 737-300 accident near Manchester Airport, GB?

A Boeing 737-300 experienced a rapid rightward swing during takeoff at Manchester Airport, leading the flight crew to abort the departure.

What aircraft was involved and where did it happen?

The accident on 2009-10-19 involved a Boeing 737-300, registration G-CELI, at Manchester Airport, GB.

What was the probable cause of the accident?

The sudden deviation from the runway centerline was caused by a large, unexpected right rudder pedal input, which the flight crew did not recall performing.

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