Engine failure and night crash during emergency landing

No fatalities • Bulverde, United States of America • Flight

An aircraft experienced a total loss of engine power following an oil pressure failure, leading to a fatal crash into trees and power lines during a nighttime emergency descent.

What happened

While cruising at 5,500 feet, the crew observed the standby power annunciator light illuminate, which was immediately followed by a drop in oil pressure. In an attempt to return to the airport, the pilot experienced a continuous decline in engine performance, eventually resulting in the propeller moving into a feathered position. During the subsequent nighttime emergency landing, the aircraft struck transmission lines and trees before crashing.

Findings

An investigation involving the disassembly of the engine's reduction gearbox scavenge pump determined that a retaining nut and tang washer had become loose within the assembly. These components moved into a position where they became lodged between the spur gears, causing the scavenge pump drive shaft to shear. This mechanical failure led to total oil starvation within the lubricating system, which triggered the loss of oil pressure and the subsequent propeller feathering.

Probable cause

A loose retaining nut and washer in the engine's scavenge pump caused the drive shaft to shear, leading to oil pressure loss and engine failure.

Frequently asked questions

What happened in the 1987-09-04 Cessna 208A Caravan accident near Bulverde, United States of America?

An aircraft experienced a total loss of engine power following an oil pressure failure, leading to a fatal crash into trees and power lines during a nighttime emergency descent.

Were there any fatalities in the 1987-09-04 Cessna 208A Caravan accident?

No fatalities were recorded in this accident.

What aircraft was involved and where did it happen?

The accident on 1987-09-04 involved a Cessna 208A Caravan, registration N807LA, operated by Martinaire, at Bulverde, United States of America.

What was the probable cause of the accident?

A loose retaining nut and washer in the engine's scavenge pump caused the drive shaft to shear, leading to oil pressure loss and engine failure.

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