1990-05-11: Piper PA-36-300 — Shelby Air Service, Inc. — Shelby, MS

Casualties unknown • Shelby, MS, US

Probable cause

THE PILOT'S INADEQUATE PREFLIGHT PLANNING AND ATTEMPTED FLIGHT WITH INSUFFICIENT FUEL ON BOARD TO COMPLETE THE FLIGHT.

— NTSB Determination

Accident narrative

THE PLT STATED THAT THE FLT DEPARTED WITH ABOUT 7 GALS OF FUEL. AFTER COMPLETING THREE SPRAY PASSES AND WHILE PULLING UP TO RETURN TO LAND, THE ENG LOST POWER AT ABOUT 150 FT AGL. DURING THE FORCED LANDING IN THE FIELD, THE WINGS & LANDING GEAR WERE DAMAGED. AN EXAM OF THE AIRPLANE REVEALED THAT THE ENG HAD LOST POWER DUE TO FUEL EXHAUSTION.

Frequently asked questions

What happened in the 1990-05-11 Piper PA-36-300 accident near Shelby, MS?

THE PLT STATED THAT THE FLT DEPARTED WITH ABOUT 7 GALS OF FUEL. AFTER COMPLETING THREE SPRAY PASSES AND WHILE PULLING UP TO RETURN TO LAND, THE ENG LOST POWER AT ABOUT 150 FT AGL. DURING THE FORCED LANDING IN THE FIELD, THE WINGS & LANDING GEAR WERE DAMAGED. AN EXAM OF THE AIRPLANE REVEALED THAT THE ENG HAD LOST…

What aircraft was involved and where did it happen?

The accident on 1990-05-11 involved a Piper PA-36-300, registration N3749E, operated by Shelby Air Service, Inc., at Shelby, MS.

What was the probable cause of the accident?

THE PILOT'S INADEQUATE PREFLIGHT PLANNING AND ATTEMPTED FLIGHT WITH INSUFFICIENT FUEL ON BOARD TO COMPLETE THE FLIGHT.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20001212X23211. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

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