AFTER INSTALLING SPARK PLUGS WITH HEAT RANGES COLDER THAN SPECIFIED BY THE ENGINE MANUFACTURER AND ADJUSTING THE LEFT MAGNETO 10 DEGREES BEFORE ITS SPECIFIED ADJUSTMENT THE AIRCRAFT WAS RELEASED FOR FLIGHT. THE PILOT TOOK OFF FOR HIS NON SCHEDULED PART 135 FLIGHT. ENROUTE THE ENGINE LOST POWER AND THE AIRCRAFT BEGAN TO DESCEND. THE PILOT MADE A FORCED LANDING IN A DRY LAKE BED. THE LANDING SURFACE WAS TOO SHORT AND THE LEFT LANDING GEAR COLLAPSED AS THE PILOT ATTEMPTED TO STEER THE AIRCRAFT AWAY FROM A STEEP BANK.