1994-05-05: Douglas DC-9-32 — Northwest Airlines, Inc — Memphis, TN

Casualties unknown • Memphis, TN, US

Probable cause

THE FATIGUE FRACTURE OF THE COMBUSTION CHAMBER OUTER CASE. A FACTOR WAS THE MANUFACTURER'S INADEQUATE INSPECTION CRITERIA.

— NTSB Determination

Accident narrative

DURING TAKEOFF, AN UNCONTAINED FAILURE OF THE LEFT ENGINE OCCURRED. AN EXAMINATION REVEALED A FATIGUE FRACTURE THROUGH A REAR FLANGE BOLT HOLE OF THE COMBUSTION CHAMBER OUTER CASE, AT THE THREE O'CLOCK POSITION OF THE ENGINE. THE ENGINE HAD BEEN INSPECTED IN ACCORDANCE WITH AN APPLICABLE AIRWORTHINESS DIRECTIVE; HOWEVER, THE FRACTURE OCCURRED 2,060 CYCLES PRIOR TO THE NEXT SCHEDULED INSPECTION. ADDITIONAL INSPECTION REQUIREMENTS RESULTED FROM THE EXAMINATIONS OF THE ENGINE AND THE FRACTURE.

Frequently asked questions

What happened in the 1994-05-05 Douglas DC-9-32 accident near Memphis, TN?

DURING TAKEOFF, AN UNCONTAINED FAILURE OF THE LEFT ENGINE OCCURRED. AN EXAMINATION REVEALED A FATIGUE FRACTURE THROUGH A REAR FLANGE BOLT HOLE OF THE COMBUSTION CHAMBER OUTER CASE, AT THE THREE O'CLOCK POSITION OF THE ENGINE. THE ENGINE HAD BEEN INSPECTED IN ACCORDANCE WITH AN APPLICABLE AIRWORTHINESS DIRECTIVE;…

What aircraft was involved and where did it happen?

The accident on 1994-05-05 involved a Douglas DC-9-32, registration N986US, operated by Northwest Airlines, Inc, at Memphis, TN.

What was the probable cause of the accident?

THE FATIGUE FRACTURE OF THE COMBUSTION CHAMBER OUTER CASE. A FACTOR WAS THE MANUFACTURER'S INADEQUATE INSPECTION CRITERIA.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20001206X01206. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

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