1994-11-08: Hughes 269A — Ark-la-tex Helicopters, Inc. — Monticello, AR

Casualties unknown • Monticello, AR, US

Probable cause

THE LOSS OF ENGINE POWER DUE TO A FATIGUED ROD END BOLT. A FACTOR WAS THE LACK OF SUITABLE TERRAIN FOR LANDING.

— NTSB Determination

Accident narrative

DURING SPRAYING OPERATIONS THE HELICOPTER LOST ENGINE POWER AND THE PILOT ENTERED AN AUTOROTATION. DURING THE DESCENT THE PILOT BECAME AWARE OF A PILE OF LOGS IN HIS PATH SO HE EXTENDED THE GLIDE. TOUCHDOWN WAS MADE TO THE ONLY SPACE AVAILABLE AND THE AIRCRAFT SANK INTO SOFT/WET MUD AND ROLLED ONTO ITS SIDE. AN EXAMINATION OF THE AIRCRAFT REVEALED THE LOSS OF ENGINE POWER WAS DUE TO A FAILED PISTON ROD END RETAINING BOLT.

Frequently asked questions

What happened in the 1994-11-08 Hughes 269A accident near Monticello, AR?

DURING SPRAYING OPERATIONS THE HELICOPTER LOST ENGINE POWER AND THE PILOT ENTERED AN AUTOROTATION. DURING THE DESCENT THE PILOT BECAME AWARE OF A PILE OF LOGS IN HIS PATH SO HE EXTENDED THE GLIDE. TOUCHDOWN WAS MADE TO THE ONLY SPACE AVAILABLE AND THE AIRCRAFT SANK INTO SOFT/WET MUD AND ROLLED ONTO ITS SIDE. AN…

What aircraft was involved and where did it happen?

The accident on 1994-11-08 involved a Hughes 269A, registration N10415, operated by Ark-la-tex Helicopters, Inc., at Monticello, AR.

What was the probable cause of the accident?

THE LOSS OF ENGINE POWER DUE TO A FATIGUED ROD END BOLT. A FACTOR WAS THE LACK OF SUITABLE TERRAIN FOR LANDING.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20001206X02592. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

Loading the flight search…