Engine power loss and forced landing involving Cessna aircraft

Casualties unknown • Topeka, KS, US

A pilot performed an emergency forced landing in a field after experiencing a loud backfire and subsequent engine power loss during takeoff.

What happened

Shortly after departing runway 18, the pilot reported hearing a single loud bang, described as sounding like a backfire. Immediately following this sound, the engine lost power. The pilot subsequently selected a nearby field to perform a forced landing. During the landing sequence, the nose gear collapsed, which resulted in substantial damage to the aircraft.

The investigation

An examination of the engine was conducted to determine the cause of the power loss. Investigators found that the crankshaft gear had separated from the crankshaft and was loose within the accessory case. Specifically, the upper portions of five of the six screws used to secure the gear to the crankshaft were located inside the accessory case.

A metallurgical examination of the fracture surface showed signatures consistent with fatigue fractures. One screw was sectioned and tested for hardness, yielding results of 29, 30, 30, and 31 Rockwell C hardness (HRC). According to TCM, the technical drawing specifies an H5 fastener with a required hardness of 32 through 37 HRC. Additionally, the head of the screw measured 0.40 inches or less in diameter, whereas the TCM drawing specifies a diameter of 0.44 inches. TCM indicated that these discrepancies could have resulted in inadequate torque during the installation. An examination of the engine and flight controls revealed no other anomalies.

Probable cause

The engine power loss was caused by the separation of the crankshaft gear from the crankshaft due to fatigue fractures, potentially resulting from improper torque during installation caused by non-compliant fasteners.

All Beech 35 accidents →

Frequently asked questions

What happened in the 2007-04-09 Beech 35 accident near Topeka, KS?

A pilot performed an emergency forced landing in a field after experiencing a loud backfire and subsequent engine power loss during takeoff.

What aircraft was involved and where did it happen?

The accident on 2007-04-09 involved a Beech 35, registration N460B, operated by ON File, at Topeka, KS.

What was the probable cause of the accident?

The engine power loss was caused by the separation of the crankshaft gear from the crankshaft due to fatigue fractures, potentially resulting from improper torque during installation caused by non-compliant fasteners.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20070412X00403. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

Loading the flight search…