Contamination in Bleed Air System Leads to Emergency Descent of Air Nippon Boeing 737

Casualties unknown • Approximately 60NM SE of Kushimoto VORTAC, JP

An Air Nippon Boeing 737-500 experienced an abnormal cabin depressurization while cruising at 37,000 feet, forcing an emergency descent and automatic oxygen mask deployment.

What happened

On July 5, 2006, an Air Nippon Co., Ltd. Boeing 737-500, registration JA8419, was operating a scheduled flight from Fukuoka Airport to Narita International Airport. While cruising at 37,000 feet approximately 60 nautical miles southeast of Kushimoto VORTAC, the flight crew observed a master caution light and an air conditioning system warning. Simultaneously, the bleed air systems from both engines ceased supplying air, causing the cabin altitude to rise rapidly.

As the cabin altitude climbed toward 10,000 feet, the cabin altitude warning horn sounded, and the aircraft's passenger address system began broadcasting automated emergency announcements. The oxygen masks in the cabin automatically deployed as the cabin altitude exceeded 14,000 feet. The crew declared an emergency and initiated a rapid descent to 10,000 feet. The aircraft subsequently landed safely at Chubu International Airport. There were no injuries among the 46 people on board, which included 41 passengers and 5 crewmembers.

The investigation

The investigation focused on why the bleed air systems failed and why the overheat switches activated. Investigators examined the pneumatic system components, including the pressure control valves (PCVs) and pre-coolers. The examination revealed traces of water ingress and significant contamination within various bleed-related valves and components.

Technical analysis of the engine maintenance history showed that a water wash for gas path cleaning had been performed during a previous C-check. Investigators found evidence that water and detergent from this cleaning process had entered the bleed air manifolds and subsequently moved into the control lines. Furthermore, the investigation looked into the effects of leaving the engines idle for several days following the washing process, which allowed the liquid residue to dry into a solid, obstructive substance.

Probable cause

The depressurization was caused by the activation of overheat switches, which shut down the bleed air supply. This was triggered when a change in engine power caused high-temperature air to flow into the pre-coolers without sufficient cooling. The switches activated because the control valves were operating sluggishly due to contamination deposits, which originated from water and detergent left in the system after an engine water wash.

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Frequently asked questions

What happened in the 2006-07-05 Boeing 737-500 accident near Approximately 60NM SE of Kushimoto VORTAC, JP?

An Air Nippon Boeing 737-500 experienced an abnormal cabin depressurization while cruising at 37,000 feet, forcing an emergency descent and automatic oxygen mask deployment.

What aircraft was involved and where did it happen?

The accident on 2006-07-05 involved a Boeing 737-500, registration JA8419, operated by Air Nippon, at Approximately 60NM SE of Kushimoto VORTAC, JP.

What was the probable cause of the accident?

The depressurization was caused by the activation of overheat switches, which shut down the bleed air supply. This was triggered when a change in engine power caused high-temperature air to flow into the pre-coolers without sufficient cooling. The switches activated because the control valves were operating…

Investigation report by the Japan Transport Safety Board (JTSB). Original record: https://jtsb.mlit.go.jp/eng-air_report/JA8419.pdf. This page is a structured re-presentation; facts and quotes are in the Japan Transport Safety Board (JTSB) - Ministry of Land, Infrastructure, Transport and Tourism.

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