Engine Failure Due to Scavenge Pump Mechanism Failure

Casualties unknown • Bulverde, TX, US

Aircraft experienced progressive engine power loss and oil pressure failure at cruise altitude, leading to a controlled flight into terrain during an attempted emergency landing.

What happened

The aircraft was operating at a cruising altitude of 5500 feet when the standby power annunciator light illuminated. This warning was immediately followed by a complete loss of oil pressure. The pilot initiated a return toward the airport; however, the engine experienced a progressive reduction in power output. Concurrently, the propeller moved to a feathered position. During the subsequent emergency landing attempt at night, the aircraft struck overhead power lines and trees before crashing.

The investigation

A detailed teardown of the engine was conducted to determine the root cause of the mechanical failure. Disassembly of the reduction gearbox scavenge pump revealed that a retaining nut and tang washer located inside the pump had backed off from their intended position. These components lodged between the spur gears, which caused the scavenge pump drive shaft to shear. This mechanical separation resulted in the total loss of oil pressure, which allowed the propeller system to feather automatically.

Probable cause

The backing off of a retaining nut and tang washer within the reduction gearbox scavenge pump, which led to a sheared drive shaft, loss of oil pressure, and subsequent propeller feathering.

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Frequently asked questions

What happened in the 1987-09-05 Cessna 208 accident near Bulverde, TX?

Aircraft experienced progressive engine power loss and oil pressure failure at cruise altitude, leading to a controlled flight into terrain during an attempted emergency landing.

What aircraft was involved and where did it happen?

The accident on 1987-09-05 involved a Cessna 208, registration N807LA, operated by Martinair, at Bulverde, TX.

What was the probable cause of the accident?

The backing off of a retaining nut and tang washer within the reduction gearbox scavenge pump, which led to a sheared drive shaft, loss of oil pressure, and subsequent propeller feathering.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20001213X32079. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

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