Hard Landing Following Pilot Intervention During Approach

Casualties unknown • Manaus, BR

A flight crew experienced a hard landing during an early morning approach due to uncoordinated control inputs by the pilot in command.

What happened

The flight crew was performing a landing approximately 30 minutes after local sunrise. The approach involved significant glare from the sun, which prompted the flying pilot to install a windshield sun shade at the other marker. During the descent, the crew performed the standard 1,000-foot and 500-foot callouts, confirming the runway was in sight.

As the aircraft descended to approximately 1,000 feet, visibility decreased due to increasing glare and low haze. While the flying pilot maintained what they believed to be the correct landing attitude, the non-flying pilot in command (PIC) took control of the aircraft prior to touchdown. The PIC attempted to flare the airplane; however, this maneuver caused the sink rate to increase. Consequently, the aircraft experienced a hard landing.

The investigation

Data retrieved from the Flight Data Recorder (FDR) confirmed the severity of the impact, showing that the touchdown produced 2.77 Gs. Analysis of the flight data indicated that the sink rate increased specifically when the non-flying pilot moved the control column aft in an attempt to execute a flare.

Probable cause

The pilot in command took control of the aircraft prior to touchdown and applied an improper aft control input, which increased the sink rate and resulted in a hard landing.

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Frequently asked questions

What happened in the 1997-03-22 Boeing 747-269B accident near Manaus, BR?

A flight crew experienced a hard landing during an early morning approach due to uncoordinated control inputs by the pilot in command.

What aircraft was involved and where did it happen?

The accident on 1997-03-22 involved a Boeing 747-269B, registration N707CK, at Manaus, BR.

What was the probable cause of the accident?

The pilot in command took control of the aircraft prior to touchdown and applied an improper aft control input, which increased the sink rate and resulted in a hard landing.

Investigation report by the U.S. National Transportation Safety Board (NTSB) historical archive. Original record: https://carol.ntsb.gov/event/20001208X07499. This page is a structured re-presentation; facts and quotes are in the National Transportation Safety Board (NTSB), United States.

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